Stainless Housings: thing of beauty.
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Joined: Apr 2003
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From: Cummins Technical Center, IN
Stainless Housings: things of beauty.
There are neat pics. Sorry if you were expecting pics of an HTT. No, these are the Stainless V-band housings for the Garrett turbos you might use as a primary in twins.
Check these out:

I'm guessing this would make twins plumbing simpler:


The rest of the pics are here
I'm expecting that these housings and their superior thermodynamic properties will allow me to run a GT4508 and get the spoolup of a GT4202
How cool is that?
Check these out:

I'm guessing this would make twins plumbing simpler:


The rest of the pics are here
I'm expecting that these housings and their superior thermodynamic properties will allow me to run a GT4508 and get the spoolup of a GT4202
How cool is that?
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If one calculates the time a volume of exhaust gas is in the housing(from when it enters till when it exits) I doubt that there is enough time to reap any benefit from a material change. By a stainless housing because it won't rust as much. Been there, done that, saved the receipt.
Ron
Ron
I would want the exhuast housing as hot as possible, thus keeping the exhuast as hot as possible. The actual egt is the same, if your comparing the same turbo and size. The energy kept in the exhuast (heat) will help drive the turbo. I deally the housing could be the same temp as the exhuast, but if its cooler, then the exhuast is being cooled by the housing. The exhuast time in the housing is shorter the hotter it gets because of its need to go from a high pressure to low pressure , that being ambient at the exit of the exhuast system.
Luckily out exhuast tracks are so short that very little heat is lost anyways, so in the real world Im confident its not measurerable or even worth going into. The only real world concern is reliabilty.
Hey cppr busa.....I have a candy red busa too.
Luckily out exhuast tracks are so short that very little heat is lost anyways, so in the real world Im confident its not measurerable or even worth going into. The only real world concern is reliabilty.
Hey cppr busa.....I have a candy red busa too.
Thread Starter
Registered User
Joined: Apr 2003
Posts: 6,564
Likes: 6
From: Cummins Technical Center, IN
-- Less thermal conductivity. Even if you had the same mass of Stainless as cast iron, it would conduct less heat, leaving more to drive the turbine.
-- Less restriction. The transition from round piping to T4 divided flange is pretty turbulent and ugly compared to a neat V-band round coupling.
In other words, this should spool better than a 1.15 A/R GT4202, but give you 110lb/min instead of 90 like a GT4202.
For the operating goal I have in mind, this turbo would be right smack in the middle of its center efficiency island pushing 80lb/min at around 2.75PR.
Drive pressure is definitely a concern with this tight of a housing, but I'm hoping that the larger turbine will keep DP manageable, remember that the same A.R on a larger turbine flows more.
I'm expecting that with a smallish A/R like this, I'll need a wastegate plumbed in for the big turbo to keep from overboosting. I could see thing thing pushing things to 60-70psi when you're only wanting 45-55.
Justin
-- lighter weight. This not only means less stress on your mount (manifold, primarily), but also less thermal mass as well. That means that the housing absorbs less heat from the drive energy, leaving more for the turbine to extract.
-- Less thermal conductivity. Even if you had the same mass of Stainless as cast iron, it would conduct less heat, leaving more to drive the turbine.
-- Less restriction. The transition from round piping to T4 divided flange is pretty turbulent and ugly compared to a neat V-band round coupling.
In other words, this should spool better than a 1.15 A/R GT4202, but give you 110lb/min instead of 90 like a GT4202.
For the operating goal I have in mind, this turbo would be right smack in the middle of its center efficiency island pushing 80lb/min at around 2.75PR.
Drive pressure is definitely a concern with this tight of a housing, but I'm hoping that the larger turbine will keep DP manageable, remember that the same A.R on a larger turbine flows more.
I'm expecting that with a smallish A/R like this, I'll need a wastegate plumbed in for the big turbo to keep from overboosting. I could see thing thing pushing things to 60-70psi when you're only wanting 45-55.
Justin
-- Less thermal conductivity. Even if you had the same mass of Stainless as cast iron, it would conduct less heat, leaving more to drive the turbine.
-- Less restriction. The transition from round piping to T4 divided flange is pretty turbulent and ugly compared to a neat V-band round coupling.
In other words, this should spool better than a 1.15 A/R GT4202, but give you 110lb/min instead of 90 like a GT4202.
For the operating goal I have in mind, this turbo would be right smack in the middle of its center efficiency island pushing 80lb/min at around 2.75PR.
Drive pressure is definitely a concern with this tight of a housing, but I'm hoping that the larger turbine will keep DP manageable, remember that the same A.R on a larger turbine flows more.
I'm expecting that with a smallish A/R like this, I'll need a wastegate plumbed in for the big turbo to keep from overboosting. I could see thing thing pushing things to 60-70psi when you're only wanting 45-55.
Justin
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