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#1 | ||
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Registered User
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Jeremy -'26 Ford Model T Roadster Hot Rod -'53 Chevrolet 210 2dr, Shaved, Nosed, Decked, Lowered, Whitewalls, SBC, AT, Full Custom -'97 Dodge 3500 DRW, NV4500, BHAF, 4" Straight Pipe, 5" Chrome Single Stack, #100 Plate FF, Starwheel FF, Isspro Guages |
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#2 | |
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Re: It wasn't a BIRD, it was a dRAG...
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It doesn't sound like anything got into the engine, so I'd check everything between the air filter and intake horn thoroughly. Maybe pressure test the system once you check the wastegate and make sure ingesting the rag and turbo bits didn't cause a leak somewhere. I'm certainly not a diesel expert - this is my first - but those are the places I'd start.
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1992 D250 CTD: A518 w/Hughes converter & TransGo TFOD-Diesel shift kit, Flex-A-Lite trans cooler under the bed, BHAF, Isspro gauges, 4" exhaust, mild pump tweaks. 100k miles 1998 Jeep TJ: Locked, lifted, Tera-low'd My Pics If aliens are so smart, why do they always abduct rednecks and wackos? |
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#3 |
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Well, I wrapped a piece of bailing wire around the flapper arm and to a bolt, keeping it shut. Went out for a test drive and it builds boost...but not like it did before. It seems really laggy.
You can hear the turbo spool up now, but it only makes about 30psi. It's still not pulling as hard as it was before all this happened with the stock H1C & 18.5cm2 housing. I can understand a drop in boost, by going with a larger turbo (HX35), but the lag is strange, since I've gone to a smaller housing (16cm2). I don't know if it's just me or what, but something just doesn't feel "right".
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#4 |
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Banned
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double/tripple check for boost leaks
Forrest |
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#5 |
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Mabye the shop towel was pluggin a leak.
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1993 D350 5-Speed, Dual 5" turnouts, Pyro, Pod's,BHAF, pump tweeked, Fixed KDP. 1992 D350 5-speed Parts truck |
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#6 |
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Im surprised ya'll havent caught this:
"I found alot of the aluminum compressor wheel pieces" Sounds alot like your turbo is shot. Be amazed it didnt snap the shaft when the rag hit it... Im amazed it still working as good as you say it is! Take a pic of the wheel.. chances are therse some good visible damage from taking in a rag. Something that spins in excess of 100,000 RPM must be balanced perfectly.. even a tiny chunk off the turbo blade will cause it to be off balance. Then you get smoking due to oil leaking past the seals as it "wobbles", youll get poor lubrication.. Even more fuel smoking when it wont make the PSI your engine wants because its wheels are no longer perfect or spinning properly..
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RIP: 99 2500 QCSB 5spd 4x4. 267k miles, SBC OFE, Comp, Stg5 Jammers, straight piped. 2007 Impala LT. |
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#7 | |
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Banned
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Quote:
brett |
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#8 |
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Timmay, I'm surprised you didn't realize this thread is over 4 years old!
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#9 | |
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Registered User
Join Date: Sep 2004
Location: INWOOD, West 'BY GOD' Virginia
Posts: 785
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Quote:
4 years ago ![]() Michael
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'92 Club auto SOLID WHITE "stripper"- rubber floor only! BHAF, 16cm, 3200GSK, ground foot, molested pump ala wannadiesel. scavanged exaust Isspro gauges in WV mount "Thats not a leak, its the external lubrication system." -JD730 "My Truck doesn't leak oil! It Sweats Horsepower!" - diesel dood Some pics of gatherings- http://community.webshots.com/user/9...host=community |
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#10 |
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OK, where is the delete button............
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1992 W350 LE reg. cab,Bullydog fuel pin slightly modified,3200 rpm ,tweaked pump, added timing, 4 inch exhaust from turbo out behind rear wheels, no muffler, BHAF, H1C/16cm with HTT Stage IV upgrade, bigger injectors,Piston LP,DTT Torque converter w/ shift kit,3:54 open axles,1999 club cab seats,reg.cab. My truck is also an alcoholic! July 2006 VA Chapter Truck of the month265hp/558 foot pounds and still looking. |
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#11 |
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Some of the rag particles made it through the intercooler and got caught up at the grid heater. A quick removal of the intake plenum and clean out the debris and everything was back up to par.
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