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#1 |
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Registered User
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Need HELP! truck running very bad
Okay so my truck has been down 5 weeks now.I welded a hanger on the exhaust straight to the frame and didnt disconnect my batteries
Im gettin brown smoke and serious rattle at idle and have no throttle response. I had a code p0088, rail pressure above max limit. I cleared it and it has not came back but it still runs the same. Here is what I have done so far with no difference:1. Disconnect batteries hopin to reset computer. 2.Took rail sensor off my buddies 05 put it on mine. 3.Disconnected the fca while the truck is running, made no difference 4. Disconnected fca on my buddies 05 to see if his ran the same as mine, it didnt, not even close he still had throttle and no where near the same sound. 5. Had Bob Wagner send me an Ecm thinkin mine was fried. 6. Smarty and mp8 both removed. Im also getting a camshaft position sensor code, I replace the sensor twice now and still got the code. Nothing has worked or made any difference whatso ever. Im lost. Anyone have ANY idea what is going on?
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Mike 06 Ram 2500 Lwb 4x4 5.9LCTD Patriot Blue Smarty tnt, Ts-mp8 Wicked 150hp nozzles Airdog 150 62/71/13ss/s400 Goerend trans. 35'' Nitto mud grapplers 10,000k HIDs 521/1037 2-20-09 suncoast dyno day 13.16 @ 102mph smarty on sw 1 |
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#2 |
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Registered User
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have removed the programmers to see if it does it stock
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SIX IN A ROW BUILT TO TOW,CUZ WELL WE ALL KNOW , HAVING A V-8 AIN'T THAT GREAT Dodge trucks that havent made life expectancy 96 3500,-175k 98.5 3500 -164k ,98.5 3500-275k, 01 3500-140k, 03 3500 -155k, 07 3500-68k waiting for possible P-Pump conversion and now I'm killing the 06,3500-116k as of 10-01-09 and counting and yes i make my trucks earn a living buy towing professionally |
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#3 |
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Registered User
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Yea forgot to add that, smarty is removed and so is the mp8
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#4 |
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Registered User
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ive welded on mine several times plus used the bed for a welding table and havent had any problems. did you check the crank sensor because the motor also reads it for the rpm's
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#5 |
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Registered User
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Havnt checked that yet, but my rpms are only reading around 200...Man I would disconnect the batteries just in case cause this crap im going through now is no fun at all. I will never take this chance again. I wonder why im not getting any other codes besides p0341..
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#6 |
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Registered User
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hey check the wirring harness for the injectors espicially the first bank mite have a short in them
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#7 |
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Registered User
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#8 |
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Registered User
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wear they go into the valve cover gasket directly to the injectors its just a rough thought
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#9 |
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Registered User
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Okay I'll check it over tomorrow, i checked ecm wires today Ill look over all of it tomorrow.
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#10 |
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Registered User
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Where did you have the ground cable attached when you welded the bracket? Check all the grounding locations and wireing harness for melted or soft spots in the wire. The welder may have used you wiring harness for grounding. Power use the path of least resistance. Had this happen on a job once and the welders fried about 10K worth of equipment when welding on the steel pipeing.
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2003 2500 4x4 FASS 95/95 +2 mic cat filter +50 DDP sticks aFe stage 2 /w Proguard 7 filter aFe Blade runner, 4" Magnaflow exh Edge w/Attitude, B&M Deepsump Pan Trans Boost Pyro A-pillar kit LP & RP fuel pressure on steering col DSS steering Brace Billet triple disc converter Excell built trans - Billet input/output shafts |
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#11 | |
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Registered User
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Quote:
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#12 |
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Registered User
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Ive used all our flatbeds as welding platforms as well no problems with them. Brown smoke out of the exhaust, it sounds like a diffrent problem.
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07 5.9 CTD MegaCab 6spd 4x4, afe blade runner, 4" silver line exhaust, AFE mega cannon CAI, 5.5" revtek/pro-comp susp lift, 5100 bilsteins, BW pocket flares, eclipse diamond audio, 35.00-12.50x20 nitto m/t, 20" diamo wheels, srt hood, dual Stabilizers, Thuren Trac Bar, -o fab trac bars DTR MegaCab Club Member #260 |
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#13 | |
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Registered User
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Quote:
The truck ran excellent, I parked it, welded the exhaust hanger back on, Fired it up and it was running like this. An hour after I had shut it up to begin welding this is what i got now I appreciate the replys from everyone..Im positive welding caused it, ran great till i struck an arc on it I would just be extremely careful welding on it now bud, this is no fun at all, ill never weld on another vehicle again unless the battery is un hooked. |
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#14 |
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Registered User
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Sounds stupid and I'm sure you already did this, but......
Have you looked over all the fuses? I know that if you arc across the alternator, it will just blow a fuse.
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'03 QC SW 4X4 |
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#15 |
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Registered User
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Doesn't sound stupid at all man, any advice is great cause i could have missed the obvious, but no i checked all the fuses. Unless there are some more that i could have missed? I didnt see any in the truck only under the hood but i pulled everyone of them and checked.
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