Performance and Accessories 2nd gen only Talk about Dodge/Cummins aftermarket products for second generation trucks here. Can include high-performance mods, or general accessories.

Got the truck up and running again, got 18.5MPG!

Thread Tools
 
Search this Thread
 
Old 04-12-2006, 09:29 PM
  #1  
Registered User
Thread Starter
 
Bobcat698's Avatar
 
Join Date: Mar 2005
Location: Amherst, WI
Posts: 1,146
Likes: 0
Received 0 Likes on 0 Posts
Got the truck up and running again, got 18.5MPG!

Got the truck back up and running after being down 2+ weeks with a blown headgasket. Ended up buying a POS car to drive for awhile.. Truck is a daily driver..

Anyways after a few hickups and about 10 flushes of the cooling system I finally got all the oil out of the cooling system, its pretty clean now!

I cranked the SP 66 up to 44PSI (I wanted 50, but it takes a lot more turns on the wastegate I guess)

I put a set of A1 head studs in.. It was not a fun ordeal due to the fact that every valve cover required grinding, a few studs did as well.
I also got the head O-Ringed and a complete valve job as well.. Head needed a bit of milling.. I could have ran a .010 headgasket but due to availability I ran a .020 headgasket.

Truck is running very well now.. Turbo cleans up much of the fuel on the top end, and low end power is much better now.. (thats with a 100 plate and laser cut delivery valves+DDP stage 4s)
I think that when I had the truck dyno'd and put down 485HP, the headgasket was already blown, hindering my numbers, but I'm not sure...

Yesterday I drove down to Goerends again to have some adjustments done to the tranny.. We put a lockup switch in as well.
On the way home, driving between 60 & 73MPH, I got 18.5MPG. Thats with 4.10 gears and 315/75/16 tires.. A new high number for me, I'm very happy with it!

Thanks again to Travis G (TDR & DTR member) & my girlfriend Le Rae for help on the project and driving me all over creation for parts!
Old 04-12-2006, 10:03 PM
  #2  
Registered User
Thread Starter
 
Bobcat698's Avatar
 
Join Date: Mar 2005
Location: Amherst, WI
Posts: 1,146
Likes: 0
Received 0 Likes on 0 Posts
Also, the truck has no problem doing this now:
Old 04-13-2006, 12:00 AM
  #3  
Registered User
 
WideOpenThrottl's Avatar
 
Join Date: Aug 2005
Location: Minnesota area/Fargo
Posts: 204
Likes: 0
Received 0 Likes on 0 Posts
What did you end up doing about the scratched up cylinders?
Old 04-13-2006, 09:03 AM
  #4  
Registered User
Thread Starter
 
Bobcat698's Avatar
 
Join Date: Mar 2005
Location: Amherst, WI
Posts: 1,146
Likes: 0
Received 0 Likes on 0 Posts
Originally Posted by WideOpenThrottl
What did you end up doing about the scratched up cylinders?
Nothing, I left it as is.
Old 04-13-2006, 09:12 AM
  #5  
Banned
 
getblown5.9's Avatar
 
Join Date: Jan 2005
Location: Baltimore, MD
Posts: 2,997
Likes: 0
Received 0 Likes on 0 Posts
i wish i could leave those black marks...but with my lag by the time i get spooled i have to shift again...

all that may change this week if i can get ahold of this htb2 64/14
Related Topics
Thread
Thread Starter
Forum
Replies
Last Post
Steven K
3rd Gen Engine and Drivetrain -> 2007 and up
4
06-04-2009 10:32 AM
b84u
12 Valve Engine and Drivetrain
7
02-20-2006 01:04 PM
icrider
3rd Gen Engine and Drivetrain -> 2003-2007
10
02-08-2006 11:12 PM
NJMurvin
3rd Generation Ram - Non Drivetrain - All Years
14
05-29-2005 09:32 PM
Sean S
24 Valve Engine and Drivetrain
11
11-15-2002 12:25 PM



Quick Reply: Got the truck up and running again, got 18.5MPG!



All times are GMT -5. The time now is 04:07 AM.